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SFB 1029 (TurbIn), B01
Active flow control in a compressor stator under highly unsteady inflow and outflow conditions
This project is part of the research cluster SFB1029 TurbIn - Substantial efficiency increase in gas turbines through direct use of coupled unsteady combustion and flow dynamics.
At the annular cascade strongly three-dimensional secondary flow develop at the blade-wall-intersection, which is pronounced stronger at the hub than the tip, due to higher loading. To further develop the active flow and closed loop control approaches of the first funding period, this asymmetric flow pattern is simulated in the 2D cascade using a contoured wall while for the annular cascade a 3D blade design is developed to relieve the hub region. In addition to the periodic throttling due to the CVC, the influence of rotor-stator interaction is investigated for active flow control. In addition, trailing edge blowing developed in TP B06 is transferred to the annular cascade and tested in combination with the side wall blowing. Furthermore, experimental and numerical investigations of different concepts of adaptive blade using piezo actuators are validated and verified on the modified 2D-cascade. The results from the 2D-cascade are used to development a design concept of a measuring section for the 3D-test rig to investigate the suitable piezoelectric adaptive blade.
Poster_SFB_B01
Person of contact: Dipl.-Ing. Jan Mihalyovics
Person of contact: Dipl.-Ing. Christian Brück
References
- Numerical and Experimental Investigations for Super Sonic Active Flow Control in the Transonic Mach Regime
C. Ebert, J. Mihalyovics, M. Staats, D. Peitsch, J. Weiss
Deutscher Luft- und Raumfahrtkongress 2019,
Darmstadt, Germany, September 30 - October 02, 2018, DocumentID: 490165,
https://doi.org/10.25967/490165 .
- A Qualitative Comparison of Unsteady Operated Compressor Stator Cascades with Active Flow Control
M. Staats, J. Mihalyovics, D. Peitsch
Active Flow and Combustion Control 2018,
Berlin, Germany, September 19-21, 2018,
https://doi.org/10.1007/978-3-319-98177-2_6 .
- Aerodynamic and Experimental Investigations on Optimized 3D Compressor Airfoils
J. Mihalyovics, C. Brück, M. Meyer, I. Vasilopoulos, D. Peitsch
ASME Turbo Expo 2018,
Oslo, Norway, June 11-15, 2018, GT2018-76826,
https://doi.org/10.1115/GT2018-76826 .
- Experimental Investigations on Highly Loaded Compressor Airfoils with Different Active Flow Control Parameters
C. Brück, J. Mihalyovics, D. Peitsch
Global Power and Propulsion Society Forum Montreal 2018,
Montreal, Canada, May 7-9, 2017, GPPS-2018-54,
https://doi.org/10.5281/zenodo.1343489 .
- Experimental Investigations on Highly Loaded Compressor Airfoils with Active Flow Control under Non-Steady Flow Conditions in a 3D-Annular Low-Speed Cascade
C. Brück, C. Tiedemann, D. Peitsch
ASME Turbo Expo 2016,
Seoul, South Korea, June 13-17, 2016, GT2016-56891,
https://doi.org/10.1115/GT2016-56891 .
Zusatzinformationen / Extras
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Dipl.-Ing. Jan MihalyovicsTel. +49 (0)30 314-29481
Institute of Aeronautics & Astronautics
Room F 013
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